A Serline ChuckTooling for my Taig lathe
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the Making Stuff collection
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You can buy 5/32 inch thick precision flat washers to fit the Taig spindle nose. With such a washer, the Sherline chuck screws on and registers against the washer which registers against the reference face of the spindle. This works, but when I compared my Taig chuck with the Sherline chick, I saw that the total thickness of the back of the chuck is the same. The Taig chuck has fewer threads because the back 5/32 of the threaded hole is bored out to to fit the unthreaded portion of the spindle nose.
I carefully measured the length of the Taig spindle nose to verify that
it would not interfere with the chuck mechanism if I screwed it in all the
way, and then decided to take on the job of boring the back of the Sherline
chuck to match the way Taig chucks are bored.
The photo of my mandrel also shows the shoulder on the Taig spindle. The reference face of the spindle is the flat rightward-facing surface of the hexagonal portion of the spindle. The threads on the spindle nose stop well before they reach the reference surface.
With the mandrel trued up, I checked that the face of the Sherline chuck jaws
was no longer than the trued up surface of the mandrel. Fortunately, they were
very close to the same length, so I mounted the chuck on the mandrel with its
back open to the world.
Because the chuck jaws are clamping a fixed mandrel and
you are moving the chuck body, all the screw motions are backward, but with
work, I got it dialed in to under a mil of runout. The runout at the very
back, by the reference face, is what matters most, since this is the point
concentric with the very short bore we want to make.
That's why the photo shows the indicator finger running so far from the chuck
jaws.
The photo to the right shows the setup for boring the recess. I set the tip of my boring bar against the reference face of the chuck, then used a 5/32 allen wrench as a spacer while I adjusted the carriage depth stop. The red arrow in the photo shows the allen wrench pinched between the depth stop and the lathe carriage.
The boring bar is adjusted very close to parallel to the the lathe axis — the cutting edge of my bar is relieved behind the tip, so setting the bar this way bores to an almost flat face.
With the allen wrench removed, I adjusted the depth of cut so the boring bar
would take a shallow skim cut off of the threads in the bore of the chuck.
I repeated taking off skim cuts until my caliper showed that I'd opened the
bore to just over 3/4 of an inch.
After I chamfered the end of the threads, I also chamfered the opening of the bore. My chamfer there was minimal, about half the depth of the chamfer on that point on my Taig chuck. The photo here was taken after finishing the two chamfering cuts and cleaning out the swarf.
After removing the chuck from the mandrel, I tried to screw the chuck onto
the spindle and failed. After re-cleaning the bore and using a scraper to
try to remove any burrs from the cut ends of the threads, it still didn't
screw on. The solution was to chase the threads using a borrowed
3/4-16 tap.
Chucking a piece of drill rod in the jaws, however, I found that the rod was not held on axis. Zeroing the runout at the chuck end of the rod left the far end wobbling visibly when I turned on the lathe. There are three possibilities:
All of the photos here that show the back of the chuck show significant rust. I cleaned the back of the chuck very carefully, wiping it down with a solution of white vinegar and salt to remove the rust, then wiping it with clean water to remove the acid and salt before using an oil wax mixture to seal it against further rust. All of this was done very carefully to keep water, vinegar and salt from getting anywhere but on the reference surface at the back of the chuck.
I also took the opportunity to remove, clean and replace all of the jaws and jaw adjusting screws. I did this one jaw at a time so as not to interchange the jaws from their original slots. There was significant gunk to clean out of the slots. I found that two jaws, even after re-cleaning, refused to slide smoothly in their slots, but each slid smoothly in the other slot. I opted to exchange those two jaws, and then I oiled the screws and jaws. It was at this point that I first noticed some of the damage to the jaws and chuck; see the next section for more on this.
With the jaws cleaned and back in place, I mounted the chuck and studied it with my dial test indicator. What I found was reassuring. The face of the chuck indicates flat to within a mil all around its perimeter. The work-facing flats on the jaws are not quite as good, but they are within a 2-mil range. These measurements leave me content that my boring on the back of the chuck was successful.
However, when I clamped my drill rod in the chuck and dialed it in to under a mil of runout at the chuck, it still wobbled considerably at the far end. I repeated this experiment with three different drill rods, all with the same result.
Conclusion: My chuck jaws are not ground to hold work parallel to the lathe
axis. I need to skim off the inside faces of the jaws with a grinder to
fix this.
The chuck body is not hardened, so it was a simple matter of using number
stamps and a small hammer to number the slots. The jaws, on the other hand,
are hardened, so I used a diamond point in a dremel tool to mark the sides
of the jaws.
That is not all, there's a big flake taken out of the shoulder of slot 1 in the chuck. It's impossible to say if this flake came from the same crash or a different crash, but something hit the jaw in slot 1 hard enough that the far side of the jaw cracked the steel chuck body and sent a steel flake flying.
Looking back at the photos distributed with the original e-bay listing, both the damage to the jaws and the flake taken out of the chuck body are visible, if you know what you are looking at, but not at all obvious. I certainly didn't notice when I put in my bid. With the jaws in the chuck as they were in the listing photo, they just looked a bit worn, an the flake could have been a shadow.
If the jaw and chuck body damage were caused by the same accident, given the point of impact on the jaw, the chuck must have been holding something very small. That, in turn, would justify spinning it at the kind of high RPM that could lead to such severe impact damage.
The big question, on finding this damage, is simple. Is the chuck still usable? I mounted it back on the lathe spindle, minus jaws, mounted my dial test indicator on the toolpost, and carefully adjusted things so that the chuck jaw slot was exactly horizontal, with the finger of the DTI resting on the jaw guide within the slot.
Driving the cross slide in and out, I measured each of the 8 jaw guides and
found that none of them were distorted. That suggests that the chuck is still
usable. I should probably try to do the same on the 8 inside surfaces of the
jaw guides, but my DTI finger is not long enough for that.
Recall that when I started out, I found that two jaws didn't slide well in their slots and switched them. I'm pretty sure that I switched the jaws now numbered 1 and 2. That means that the jaw now numbered 2 was in the slot now numbered 1 when I got the chuck. Both those jaws are chipped, but but the damage to jaw 1 seems greater, making me guess that I restored it to the slot it was in at the time of the crash.
Did someone, after the accident, switch the jaws (perhaps unintentionally)
and then try to repair some damage by sticking a grinder down the throat
of the chuck? It's hard to say, but it's also apparent that whoever did that
didn't do a very good job. I'll see if I can do better.